Firstly, we wish all our members and supporters a very happy 2024, it promises to be a very busy and important one for 35011 General Steam Navigation, as we prepare, finalise and submit our National Lottery Heritage Fund application, we are working extremely hard behind the scenes with strategic application partners to meet the rapidly deadline of June 2024!
This has now been cleaned and inspected, The news is not all bad, but as we intend to run on the main line we have to juggle repairing verses replace. The front tube plate will need replacing, and some, if not all, of the rear tube plate will need replacing. Crucially, the boiler barrel itself is fine, though it may require some small bits of work. The firebox will need a replacement bottom edge as the metal is too thin, all the repair welds will need checking as they are indicative of cracking. So we probably look to replace the box entirely.
Frames
As part of the process of preparing the frames for unrebuilding, we are slowly removing, cleaning up and replacing the “nuts and bolts”
retaining the cylinders to the chassis where possible.
It is a slow process, many of the bolts have not been moved since 1959, but it will save money and time later when we are ready to install the new middle cylinder.
Similarly, our volunteers have been cleaning up the frame stretchers, so we can better assess their condition and suitability for
retention or replacement.
Leading bogie
Our volunteers have been prepping the leading bogie for restoration and preparation for mainline running. The general condition of the
bogie is good, we are working on releasing the side control unit,
and the rest of the bogie is ready for restoration. As discussions and thoughts around installing European Train Control System (ETCS) coalesce (more information in The Packet) we may need to add some bracketry to the bogie to mount the forward Balise Transmission Module.
Behind the scenes As well as just the visible physical engineering our Engineering sub committee have of course also been very heavily involved in producing the over 17 work packages, to date that detail the specifications and costs to support our National Lottery Heritage Fund application
If you are also interested in getting involved more directly with the Engineering side of the project in any way, especially if you have any experience with Bulleid pacifics (but not essential) Contact Us here.
Welcome to this Summer 2023 engineering update from the General Steam Navigation project. Progress has been made on various engineering fronts on the project over the past few months and with some of our background efforts about to bear fruit we’ll have some brilliant work to share over the coming months.
Boiler Since the last packet, there has been no further progress on the boiler, but we are working on scheduling the boiler washout. This was originally planned for February, but was postponed due to a combination of personal circumstances. Mother nature had a go at helping with the washout recently, but photos from inside the boiler show everything remains dry. The Boiler washout actually took place at the beginning of August with the grateful assistance of our friends within the Swindon & Cricklade Railway Steam loco department. Details of the Boiler Inspectors preliminary inspection report will be in the next issue of our Members Magazine The Packet, if you not already a member join here today to get the latest news first.
Trailing Truck Progress on the trailing truck has been slim since provided in the last Members Magazine The Packet, as the NNRE have had other tasks taking higher priority. Following the previous issue of The Packet, we have had some helpful insight into the weldability of gunmetal (and leaded gunmetal) which is proving very useful.
Crank Axle Physical progress with the crank axle continues to be impacted by geopolitical events causing volatility in the price of steel, after discussions with our friends in the B17 Steam Locomotive Trust project & A1 Steam Locomotive Trust, with whom we were planning to place a group order for A4T forgings for the stub axles, we are pausing the ordering process until we have greater certainty over the price. Whilst it is disappointing to not be placing an order for these crucial parts of our locomotive, it feels more prudent to wait, saving us money in the long run. During this self-imposed delay, we continue to use the time to produce the engineering justification for manufacture of the stub axles in A4T & the sweep webs in 817m40, so that when we are happy with prices, we can proceed.
We are also continuing with the initial design of the new chain-driver sprocket to fit the balanced crank axle design. The design fitted to the original unbalanced crank won’t fit the balanced crank design, as the stub axles are wider & the mounting points were changed. There was a design for the sprocket for the balanced crank axle, but it is not in any drawing collection that we are aware of, and is assumed lost. The design we are working on will be based upon the original sprocket along with the mounting design for the eccentric fitted on rebuilding to drive the inner motion, as we know the mounting points were broadly the same.
Leading bogie
Work has started on taking off the removable parts of the bogie, to reduce the work that would be done when it is sent away. The key component is the side control unit. Our leading bogie was attached to the frames via a pin and bush arrangement, similar to the trailing truck. On both of these, the pin is firmly attached to the frame of the locomotive, but the bush can slide laterally within the side control unit. Either side of the bush is a spring in compression. As the locomotive enters a curve, the frames will want to continue in a straight line, whilst the bogie will follow the curve. This will compress the spring on the outside of the curve, and extend that on the inside of the curve, helping to steer the front of the locomotive through the curve. We have started taking the side control unit apart, so it can begin to be cleaned & restored.
Frames
The main activity at recent working weekends, beyond the leading bogie, has been on the frames. As we will eventually need to remove all three cylinders from the frames as part of the process of replacing the middle one, we are starting to remove, clean and replace/refix all the nuts & bolts that hold the cylinders to the frames.
This will mean that when we are ready to remove the cylinders, we should be able to detach them quickly. It will take some time to do this, but will save time in the long run. The middle cylinder is being replaced, with a new one to be manufactured to the original design, with outside admission. Removing the outer ones will make removing the middle one easier, and will give us the opportunity to
Welcome to this autumn engineering update from the General Steam Navigation project. Progress has been made on various engineering fronts on the project over the past few months and with some of our background efforts about to bear fruit we’ll have some brilliant work to share over the coming months.
Boiler
The boiler tubes are gone! After many months of hard work by our small band of volunteers, the job is done. Work has continued on removing rust from the inside of the firebox, descaling the inside of the boiler, and generally cleaning the inside of the boiler and firebox ahead of a planned inspection later this year. Still to do is sourcing the right tool for removing the thermal-syphon inspection plugs, so that we can wash out the boiler, and then plan the inspection.
Crank axle
Progress with the crank axle has been limited in the past few months; geopolitical events has caused the price of steel to become volatile, after discussions with our friends in the B17 project & A1 Steam Trust, with whom we were planning to place a group order for A4T forgings for the stub axles, we are pausing the ordering process until we have greater certainty over the price. Whilst it is disappointing to not be placing an order for these crucial parts of our locomotive, it feels more prudent to wait, saving us money in the long run. During this self-imposed delay, we are using the time to produce the engineering justification for manufacture of the stub axles in A4T & the sweep webs in 817m40, so that when we are happy with prices, we can proceed.
Frames
Work on the frames continues at a good pace with our volunteers working hard to clean up the frames in preparation for assessment of their condition. With over 50 years of grime to remove on the frames its not a particularly glamorous job but is very important and we are extremely grateful to all our hard workers. We have also removed the brake cylinders from the frames as they wont be required for an original condition Merchant Navy. The cylinders will be cleaned up and stored should a rebuilt Bulleid require them in the future.
Sponsorship component of the month
For those that want to make a more tangible contribution towards putting the steam back in General Steam Navigation we have relaunched the ‘Component Sponsorship’ scheme.
Each month the Society will highlight one particular component. The scheme will allow generous sponsors to cover the cost of individual parts that range from few pounds to several thousands.
Our generous sponsors will receive a certificate describing the part sponsored, be named on the roll of honour on this website and gracious thanks from all those who wish to see General Steam Navigation back in operation.
This month we are starting with the steam chest covers for the outside cylinders. The steam chest covers are a relativity simple component to produce being machined from plate steel. 35011 will require 4 of these in total with the covers being fitted to the front and rear of the cylinder on both sides .The cost of these covers are £250 each. For a full list of the currently available component and how to sponsor them please visit the component sponsorship page.
Draughting
The question that has been asked a few times, both within our project, and outside it, is why we are considering modifications to the exhaust, especially as Bulleid pacifics had a reputation for being free-steaming, if hungry locomotives. The reason is buried in that last statement. Consider how a steam locomotive, especially its combustion system works: exhausting steam in the smokebox produces a draught, sucking air into the firebox for the coal to burn. How much air the locomotive supplies to the fire will impact its fuel combustion. Too little, and you have rich combustion, which releases a lot of heat from the coal, but at the expense of high fuel consumption. Too much air, and you have overly lean combustion, which is cleaner (less production of carbon monoxide), but it can lead to high fuel consumption as well, as the extra air cools the hot air from the fire, reducing the heat transferred to the water in the boiler, meaning more coal is needed to be burnt to produce the same heat transfer to the steam. The reputation, coupled with data from the Rugby reports, suggests that at most of the steaming rates GSN is likely to operate, the combustion is too rich. The perfect air:fuel mass ratio for stochiometric combustion of coal is approximately 11.2:1. It is normal to supply more air than is necessary, to ensure all of the fuel sees sufficient air, normal practise for combustion of coal is to have approximately 30% extra air, so the ratio becomes 14.6:1. Data from the Rugby reports show the original locomotives ran with a ratio of between 11:1 & 17:1, with drop off in performance for steaming rates above 18,000lb/hr, which is where we can expect to operate. The rebuilt design exhaust was much less variable to incomplete combustion, and had higher air:fuel ratio. The data also suggests that these locomotives need to run with significant excess air, far more than the 30% recommendation. The rebuilt design can actually be seen to be broadly similar to how 71000 operated in BR service, suggesting that we can achieve similar performance with 35011 if we can emulate the performance of 71000s twin Kylchap design. By redesigning the exhaust, we should be able to achieve two things: (1) maintain closer to 50% excess air across the power range, reducing fuel consumption and (2) increase the total flow area of the blast nozzles, reducing the cylinder back pressure.
Working Weekends
Our current plan for working weekends in 2022 is as follows:
15th /16th October
12th /13th November
10th /11th December
14th /15th January 2023
11th /12th February 2023
11th /12th March 2023
As always, any members who would be interested in being involved with the engineering of our project, please do get in touch. Our CME Dr Steve Rapley does need some support on the engineering of this project, especially at the moment with weld design, so if you have any experience in this area, please do get in touch. Similarly, if you have any question or comment on the Engineering report or the engineering in general, please do get in touch at by email to Dr Steve Rapley here.
To help us achieve our goal of an original condition Merchant Navy we’ll need your help, you are able to support us in many ways if you are not already a Society member you can sign up for membership for currently only £15 per year here, or donate to the Society here, consider sponsoring a component here or even better become a shareholder here.
Since, the last trailing truck update, and arriving at the North Norfolk Railway (NNR) the truck has been fully dismantled, a detailed examination and testing undertaken.
News on the truck can perhaps be broken into 3 sections, The Good, The Bad and The Ugly” (the film being sequel/prequel to “A Fistful of Dollars”, which we need to get the project completed).
The Good
The axle & wheelset are in excellent condition. Visual and Non Destructive Testing (NDT) of the axle showed no defects. One end of the axle has some pitting, but the majority of the axle is at its original size. NNR are awaiting confirmation from Ricardo, our certification body, that we can appoint our preferred subcontractor for the tyre turning/profiling to be done.
The new set of springs that we purchased as part of an order with our friends the 35006 Locomotive Society are excellent and all have the same deflection under load, so setting up the height of the Trailing Truck will be easier.
The Bad
The Left Hand axlebox has visible cracks in three places, one of which extends at least two inches down the side and would need grinding out to near the top of the arch before attempting a welding fix, that being gunmetal could be difficult to demonstrate that it’s been adequately done. The Right Hand axlebox however has no visible cracks. The bottom of both axleboxes are bent, probably from the truck being jacked up at some stage. The LH is far worse than the RH and may well fracture if we try to return it to shape, the RH might be OK to be returned to shape. The plan is to use penetrative dye on both axleboxes to look for further cracks, but there is a good chance we will have to replace the LH axlebox.
There is a pattern available for the axleboxes, and these are the same as for the tender, so if we do decide to replace it, we may well consider ordering all eight to reduce costs (including the RH axlebox).
The Ugly
The swan necks at the front of the truck are in poor condition, especially the Right Hand one. We are recommending that they are cut out completely and replaced as the best long-term solution. We can then be certain the frame remains true, and ensure the strength & rigidity of the final frame. It will also enable NNR to examine the rear of the frame and it’s condition around where the necks are connected.
There is a small crack in the right rear of the frame, close to where the swan neck ends, but it should be repairable. We have instructed NNR to arrange for NDT around the crack, the location on the LHS of the frame and also around all the other weld areas as well, to determine how much material is there and how sound all the welds are.
Next steps
NNR are creating a full CAD of the Trailing Truck, partially to understand how the truck went together originally, as well as for replacement parts. NNR will advise us of the likely costs of the testing and the manufacture and installation of the new swan necks the replacement swan necks . We knew that only once it was fully disassembled, examined and tested that a complete picture of the work required would be obtained.
The members of the Trailing Truck Transformers group are key to funding this key component back to working order and you can help by joining our group here.
The momentum being generated by our engineering team means 2022 is going to be a very important year for the project with some big goals in mind. To achieve this we will need your help, you are able to support us in many ways if you are not already a Society member you can sign up for membership for currently only £15 per year here, or donate to the Society here or even better become a shareholder here.
Work continues on the boiler with the last of the remaining boiler tube stubs being removed last month. A big thank you goes out to the sterling work by our volunteers (including Paul G, David O, Geoff A & Jack G) who completed this strenuous task. Work has started on removing rust from the inside of the firebox, descaling the inside of the boiler, and generally cleaning the inside of the boiler and firebox ahead of a planned inspection. It may seem that one paragraph seems like little progress on the boiler, but this work is very labour intensive, and with only a small band of volunteers takes time for the fruit of their labours to become apparent.
Crank Axle
An interesting fact that has come to light recently is clear evidence that the original design for the Merchant Navy had a balanced crank axle. This was mentioned briefly in the Crewkerne report, in going through drawings of the chain- driven valve gear, one early drawing clearly shows a balanced crank axle. There are no other drawings showing this, it is understood that an unbalanced design was introduced to reduce the weight of the locomotive, but it’s interesting to think what could have been, with a balanced crank axle, Crewkerne may never have happened, which was a key driver in the rebuilding process.
Progress on designing the crank axle continues, we have now converted the original drawing into an electronic CAD file. The next step with the axle will be to design the chain-driver sprocket, for which no drawing exists of one that would fit the balanced crank, and to start conversations with a forger & manufacturer to develop forging & manufacturing drawings.
A question of balance
As progress continues with design work for the new crank axle, our thoughts are turning to the balancing design. As members will be aware, one of the changes that was obvious on a rebuilt Merchant Navy were the external balance weights on all 3 axles. Our plan is to remove the weight added in 1958 on the leading & trailing axles and rebalance the wheels with weight in the pockets again, if possible. We still need to decide on the shape & material of the coupling rods, which will impact on the amount of balancing needed on these axles, but aesthetically we want to restore that classic Bulleid appearance with no visible balancing. The central driving axle is another question. Originally the crank webs & inside connecting rod were balanced on the wheel rim, with a large plate on the rear face of the wheels and lead in the pockets. The question that arises is what would have been done to that lead when the balanced design was fitted to 35011 before rebuilding? At first inspection, one would think a significant amount of that lead would have simply been removed. However, it’s slightly more complicated than that. All steam 7 locomotives have an amount of balancing on their wheels, to counteract the rotating masses of the coupling and/or connecting rods, as well as, where necessary, the valve gear. Some locomotives, especially 2-cylinder designs, attempt to partially balance the reciprocating (backwards & forwards) masses, to reduce the front-end oscillation that occurs. This balancing can only be perfectly conducted for a given speed, so the engineer has to decide what speed to balance at, and the percentage of reciprocating masses balanced is usually limited to reduce the hammer-blow on the track from these additional rotating masses. Bulleid reasoned that for a 3-cylinder locomotive the reciprocating masses were to a certain extent self-balanced within the mechanics of the machine, as the longitudinal motion of one cylinder is always partially opposed by the other two, and so didn’t add any additional mass to balance the reciprocating forces. For stability purposes, rotating imbalances on one wheel were balanced on the other, so the left-hand balance weight balances the right-hand motion (and viceversa). By studying & understanding the designs for the original & rebuilt locomotives, we’ve managed to determine how to rebalance the driving axle; it will likely have slightly greater mass (approximately 1062 lbs vs. 942 lbs) on it than on the original design, but it will be at a different location (175° vs 140° from the crank); compared to the rebuilt design the location is similar, but the mass is reduced by around 6%. Geometrically, it can be seen how this works out in the drawing of the original design, by balancing the crank webs with counterweights, we have removed the line labelled middle (GH, the righthand side of the polygon), the closure line is then from A to G & is slightly longer than the line AH, at a shallower angle. The leading & trailing wheels from a mechanical perspective won’t need rebalancing, though from an aesthetic perspective we will plan to do this. We also plan to fit the plain rods that were fitted in 1956, as they have greater tensile strength and are less prone to bending. The next step with the balancing is finer detail; we need to determine the disposition of lead in the pockets to achieve the desired counterbalance. For the leading & trailing wheels, this is little more than a tweak to the original design. The central wheel needs some more design to determine the centre of gravity of the lead pockets and the balance weight plate, it is anticipated this will be completed in the coming weeks.
Frames update
A key event in the process of unrebuilding 35011 occurred at the November working weekend when, with the very welcome assistance of the Swindon & Cricklade Railway, and after many, many weekends of effort, the 5 large brackets that held the external valve gear & screw reverser were lifted off the frames. As we are planning to construct Bulleid’s chain drive valve gear (& fit a steam reverser) these brackets are now surplus to requirements. They are in excellent condition, so we are offering them for sale to any interested parties. By removing these, we made it easier to access other areas of the frame, and quickly removed the last of the brake blocks & arms from the leading & trailing axles. The plan now is to continue 10 removing all the parts hanging off the frames; later in 2022 we should then be able to lift the frames, releasing the leading bogie, leading axle & trailing axle. The leading bogie will then be assessed and prepared for professional restoration to mainline condition, whilst the driving wheels will be sent to South Devon Railway Engineering for rebalancing & profiling.
In order to help fund the work on the frames the Society has started a Funding the Frames appeal that will be essential for the successful restoration of GSN back into her original condition. Not only do we need to clean and review the condition of the frames as they exist today, any corroded sections of the framework, the rear platform and dragbox will cut out and replaced. We also need to reverse some of the areas that were changed during rebuilding to allow a new middle cylinder to be installed and reinstate Bulleid’s unique patented chain driven valve gear.
This a general fund with no minimum / maximum donation or number of contribution limits, all monies donated to the Fundiung the Frames appeal will be specifically ring fenced for the frames. If you are able to contribute to this project in any way however great or small, we thank you for your support. You can find out more here
University projects
We now have a further university project looking at the Internal Aerodynamics of a Merchant Navy. Building on lessons learnt last year, as well as better understanding of the test data that is available on both the original smokebox as well as the rebuilt design, they have made excellent progress simulating 3 baseline designs before moving onto some potential design improvements. The new designs they are looking at include some variations on the original exhaust design as well as variations on a Lempor exhaust, in both cases to understand the impact of nozzle size, angle & target upon the smokebox draught. Based on this work, we may run a final study in academic year 2022/3 to polish off the design as well as to understand how it impacts on the external aerodynamics of the locomotive.
Visit to Great Central & some tender parts
As part of the student project this year, I arranged a visit to Loughborough sheds with the students, to have a crawl around Rebuilt Light Pacific 34039 Boscastle. It was a very useful visit, giving the students a good insight into what they’re simulating, and why, and was also a helpful reminder as to how much pipe work and other gubbins there is on a complete locomotive. Whilst there, in chatting with their Chief Engineer, we were offered some left over parts from their tender for a very reasonable sum, including two front footsteps, two rear footsteps, two rear ladders, one tender tank filler and lid, three Vacuum Reservoir tanks with holding down straps and hardwood timber supports, one Vacuum Reservoir tank cover, one Vacuum Reservoir tank cover, 5 tender doors and two curved front corner pieces. These are all original parts from a 2nd series tender, which became spare when the tender tank was scrapped; the vacuum reservoirs are the wrong type for a Light Pacific, the footsteps & ladders were going to be reused but were inadvertently reordered as part of the manufacture of the tank. Whilst we are years from constructing our tender, and still need to flesh out our ideas for it, it is nice to be able to have some genuine parts that can one day be fitted to our machine.
We have also recently managed to purchase two electrical lamps for the locomotive, so we now have 6 lamps. The purchase of one was sponsored by one of our directors, but if you would like to sponsor the other, please do get in touch with us.
Other Engineering Progress
We have made a start on two other big engineering areas in the last few months. Firstly, members of the Engineering Sub-Committee have started creating an online Engineering Bill of Materials (EBoM). As members of the Bulleid Pacific Locomotives Association, we have access to the extensive collection of over 3000 drawings in their catalogue, but the way they are catalogued is not very easy for understanding the relationship between the drawings, nor for knowing what drawings we are missing. By producing the EBoM, in time we will be able to have a clear record of how many of each part we need, the drawings for them, records of when we order parts & how, records of manufacture where appropriate, etc. Those projects that have constructed (or are constructing) locomotives from scratch, such as 60163, 2007, 72010 have gone through a similar 13 process. By starting this, we are laying the foundations for our original Merchant Navy and starting to put the documentation in place we will need to be accepted for mainline running.
The second significant progress is in the subject of assurance, the process by which we demonstrate the locomotive meets the standards necessary for mainline running. After meetings with numerous potential assurance partners, and independent advice from others in the industry, we have appointed Ricardo Rail to be our assurance partner. They will give us the support to understand & produce the evidence we need to restore General Steam Navigation to original design conditions whilst meeting mainline standards, and document that process. They work with numerous similar projects and are a good fit for our project.
Finally, we are becoming involved in a forum of new-build steam locomotives, to look at ways of pooling knowledge and cost-saving between us. Whilst that title may bring howls of protest from some quarters, we have things we can learn from these groups in the assurance process. Where we are manufacturing components from scratch, we will need to demonstrate that the finished component doesn’t bring additional risk to the design compared to the original. Where we are restoring, we will need to demonstrate that our restoration has returned the components to a condition where it doesn’t bring additional risk to the locomotive.
As always, any members who would be interested in being involved with the engineering of our project, please do get in touch. I need some support on the engineering of this project, especially at the moment with weld design, so if you have any experience in this area, please do get in touch. We also need some additional support archiving drawings online into the EBoM, this is an opportunity to study some of the original drawings of a Bulleid pacific. Similarly, if you have any question or comment on the Engineering report or the engineering in general, please do email our CME (steve.rapley@35011gsn.co.uk)
The momentum being generated by our engineering team means 2022 is going to be a very important year for the project with some big goals in mind. To achieve this we will need your help, you are able to support us in many ways if you are not already a Society member you can sign up for membership for currently only £15 per year here, or donate to the Society here or even better become a shareholder here.
Work on General Steam Navigation has progressed at a pace over the last few months with our regular working parties at Blunsdon. The majority of the work has been focused around 35011s chassis in preparation for “crane day” that happened in November. With the help of our friends at the Swindon and Cricklade Railway steam department our volunteers were able to successfully remove the five frame hangers that won’t be required in the restoration of General Steam Navigation back to Bulleid’s original condition.
These components were: the slidebar bracket hangers (these were heavily modified upon rebuilding due to the outside valve gear) and outside motion brackets on each side; along with the screw reverser bracket on the left hand side.
In the spring of next year it is planned to remove 35011s remaining wheels and front bogie in order to enable a full assessment of her frames to be undertaken.
Preparation work for producing the components required for the chassis and the alternations to the existing metalwork is being undertaken at the moment. This will enable the work to restore the rolling chassis to be only limited by the amount of money that can be raised to pay for the work. To help this work the Society has set up a “Putting Funds into the Frames” appeal which enables people to donate as little or as much to the project with the guarantee that it’ll be spent on the frames. You can find out more here.
Supporters will be aware that when we lifted the boiler from the frames in October last year, we also lifted the rear of the frames to release the Trailing Truck. Since then, work has been undertaken to remove the majority of the components that make up the Trailing Truck.
Following an independent assessment, we undertook a competitive tender process and in August we awarded the contract for the full refurbishment, and certification of the Trailing Truck by specialist contractors North Norfolk Railway Engineering (NNE).The Trailing Truck left Blunsdon and arrived safely at NNE Weybourne on the 10th October.
Since then North Norfolk Engineering have provided the following update of their activities:
• Completed the dismantling of the main component parts, with the truck chassis now lifted off the wheelset in readiness for the complete set of main parts and wheelset being sent away for shot blasting.
• Undertaken a series of key dimensional measurements to assess the general condition and wear levels ahead of developing the engineering overhaul strategy.
• Removed the seized main pivot pin out from its bronze bush and assessed the reason for it seizing, as the bush appears has moved during its working life and rotated in the frame boss, blanking off the grease hole in the process, reducing lubrication.
The next key stage is to undertake Ultrasonic Axle Testing (UAT) of the axle and the axle to wheel interfaces to verify that no flaws are present. It will be carried out by a Rail Industry approved axle specialist early in the new year (at the same time as the annual check of all locomotives on the North Norfolk Railway to minimise cost).We are in the process of arranging the purchasing new suspension coil springs and are currently working with various suppliers. To help fund the restoration of the trailing truck the Society is offering a maximum of 30 members the opportunity to purchase a ‘Lot’ for £500. Members are welcome to purchase as many ‘Lots’ as they wish up to the maximum target amount.
Members of the Fund Group would receive a number of benefits including:
Certificate of membership of the ‘Trailing Truck Transformers’
Name engraved on a suitable brass plaque attached to the refurbished Trailing Truck
Regular updates on the refurbishment of the Trailing Truck
An invitation to a VIP day at the Swindon and Cricklade Railway to see the completed Trailing Truck once it is returned to the railway.
For details on how to become a Trailing Truck Transformer please click here.
In November our CME Dr Steve Rapley took a group of students from Loughborough University to look at the smokebox and exhaust of 34039 Boscastle. This was to aid their understanding of the geometry they’re studying as part of developing the Internal Aerodynamics and draughting of 335011 General Steam Navigation Locomotive Restoration Society. The Society would like thank Andy Morgan and Mike for hosting us.
Progress continues with the boiler, there are still some stubborn ends of tubes to remove, but it is down to a handful now. Sterling work by our volunteers (including Paul G, David O, Geoff A & Jack G) continues with this strenuous task, with the expectation that the remainder will be out in the coming months. Work has started on removing rust from the inside of the firebox, and generally cleaning the inside of the boiler and firebox ahead of a planned inspection early next year. It may seem that one paragraph seems like little progress on the boiler, but this work is very labour intensive, and with only a small band of volunteers, maintaining Covid safe practices, it takes time for the fruit of their labours to become apparent.
In order to keep moving forwards with our restoration activities, the society is looking for a qualified railway mechanical engineer, preferably with welding experience or weld design experience, to advise the CME & Engineering Sub-committee in this field. If you fit this description, or know someone who does, please get in touch with us via info@35011gsn.co.uk
The momentum being generated by our engineering team means 2022 is going to be a very important year for the project with some big goals in mind. To achieve this we will need your help, you are able to support us in many ways if you are not already a Society member you can sign up for membership for currently only £15 per year here, or donate to the Society here or even better become a shareholder here.
Last week our Chief Mechanical Engineer took a group of students from Loughborough University to look at the smokebox and exhaust of Bulleid Light Pacific 34039 Boscastle that is currently undergoing overhaul on the Great Central Railway.
This was to aid their understanding of the geometry they’re studying as part of developing the internal aerodynamics and draughting of our 35011 General Steam Navigation.
At the Annual General Meetings of the General Steam Navigation Locomotive Restoration Society (GSNLRS) and General Steam Navigation CIC we were delighted to announce that following the removal of the trailing truck from the frames in October 2020 and months of preparatory work by their hard working volunteers, that the restoration contract for the trailing truck has been awarded after a tender process to North Norfolk Railway Engineering.
Located at Weybourne Engineering works, North Norfolk Railway Engineering presented a strong bid for the work, with a high level of engineering detail, that respects the historical merit of the unique in preservation fabricated Merchant Navy trailing truck.
Originally fitted to a series 3 Merchant Navy, our fabricated trailing truck is the last survivor of its kind. Lighter than the cast truck fitted to the other preserved Merchant Navy locomotives, longer than a Light Pacific’s truck, the GSNLRS are having this unique piece of Bulleid locomotive design restored to mainline standard, a crucial step towards GSNLRS’s vision of an original Merchant Navy with original air smoothed casing and Bulleid’s patented chain driven valve gear.
For more information on the North Norfolk Railway go to: www.nnrailway.co.uk
Crank Axle Steel Selection
Since 1966, 35011 has been without it’s central crank axle. Alongside the missing valve gear, this has been the driving force behind the decision to return to original design condition, due to the cost of replacement to either design being similar.
After many years of behind-the-scenes research in the BPLA collection & National Archive in Kew, and recent detailed Finite Element Analysis conducted at the University of Birmingham, under the supervision of Professor Karl Dearn, has demonstrated that A4T steel is of a suitable grade for the correct balanced crank axle design for 35011 in original design condition.
Whilst Covid19 has been affecting both our financial and engineering efforts, the Society is delighted to report that new parts continue to be constructed. Recently the front bogie spring beams were delivered by Ashbrook Engineering Ltd; the Society is extremely grateful to Mr Alan Dixon who sponsored their construction. Along with the efforts of Mr Tony Simmonds who is machining the spring hangers for the Society, work on the bogie is progressing at a good pace.
Work continues with converting the BPLA drawings of the frames & valve gear into CAD to allow us to have replacement parts manufactured. This is a lengthy process, but one that is vital for our goal of reengineering the existing frames to a condition where they can accommodate the original chain-driven valve gear and replacing the middle cylinder. In time we will also have the drawings of the smokebox and air-smoothed casing transferred to CAD for the same reason.
The Trailing Truck Transformers funding group continues to be our primary fundraising campaign with its objective of funding the restoration of GSNs trailing truck. The Society is pleased with the initial number of members who have signed up for blocks but are under no illusions that its still along way from being funded. We are offering a maximum of 30 members the opportunity to purchase a ‘Lot’ for £500. Members are welcome to purchase as many ‘Lots’ as they wish up to the maximum target amount.
Members of the Fund Group would receive a number of benefits including:
Certificate of membership of the ‘Trailing Truck Transformers’
Name engraved on a suitable brass plaque attached to the refurbished Trailing Truck
Regular updates on the refurbishment of the Trailing Truck
An invitation to a VIP day at the Swindon and Cricklade Railway to see the completed Trailing Truck once it is returned to the railway.
We understand that £500 is a lot of money and for people who wish to support the trailing truck but are unable to join the Trailing Truck Transformers club you can help us by donating to our Wheel Set appeal on our JustGiving page here.
The 35011 Twenty Twenty Club winners have been drawn for January.
Congratulations go to:
1st Prize – David Oborn, 2nd Prize – Simon Shutt, 3rd Prize Allan Bott
The Twenty Twenty Club is a great way to help raise funds for the locomotive and at the same time have a little bit of fun. We still have the last few places remaining find out how to join here.
2021 is shaping up to be a very important year for the project with some big goals in mind. You can help support us in many ways if you are not already a Society member you can sign up for membership for currently only £12 per year here, or donate to the Society here or even better become a shareholder here.
Finally some of our trustees will be making a guest appearance on the “Railwaymania” podcast and will be answering questions from members and the general public. If you have any questions you’d like answering please send them to us on Facebook, Twitter, Instagram or through our website and we’ll ensure as are answered on the podcast as possible.
Work on the 35011 project has continued despite the latest national lockdown putting a halt to all working parties on the engine. Members will soon be receiving on their doorsteps or inboxes the latest Issue 14 of our membership magazine ‘The Packet’
This issue is over 25% larger than the previous issue with lots of exciting news from the engineering, fundraising, PR and membership teams. If you’re not a member and would like to receive a copy and be among the first to know you join our Society for just £12 by clicking here.
At our final working weekend of 2020 we were filmed & interviewed by a TV crew for a program to be aired in late 2021 which will be great publicity for our project. We have more volunteers waiting to join our working parties once social distancing becomes a thing of the past which will speed up the rate of restoration. At this moment in time GSN is a dormant creature, waiting for its time to live again and with your help we can do just that. No matter what skills you have we can use your help. Please contact our volunteer liaison officer Mr Andrew Collett at andrew.collett@35011gsn.co.uk if you fancy getting your hands dirty.
At the start of the month Hornby announced that a new model of General Steam Navigation will be joining the Hornby Dublo range. The model will be limited to 500 models and feature a diecast boiler. The locomotive is wearing the BR Brunswick green livery and looks brilliant. You can find out more on the Hornby website here.
The 35011 Twenty Twenty Club winners have been drawn for November and December.
Congratulations go to:
December 2020 – 1st Prize – Chris Mileman, 2nd Prize – David Oborn, 3rd Prize – Andrew Collett
November 2020 – 1st Prize – Chris Mileman, 2nd Prize – Steve Raply, 3rd Prize – Simon Strachan
The Twenty Twenty Club is a great way to help raise funds for the locomotive and at the same time have a little bit of fun. We still have the last few places remaining find out how to join here.
2021 is shaping up to be a very important year for the project with some big goals in mind. You can help support us in many ways if you are not already a Society member you can sign up for membership for only £12 per year here, or donate to the Society here or even better join us as a shareholder here.